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Case Study: Luxury Portable Toilet Trailer Leaking Wastewater Holding Tank Repair

The wastewater holding tank of a luxury toilet trailer undergoes repair and refurbishment
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Repair and refurbishment helps a portable toilet company avoid flushing two working luxury trailer units down the drain

Holding tanks with the capacity to store 3000 litres of wastewater underneath two luxury portable toilet trailers undergo repair and strengthening after the metalwork became weakened by corrosion, causing numerous holes to appear.

Case Study Data


Site
Luxury Portable Toilet Trailer
Location
United Kingdom
Repair Type
Tank repair and refurbishment
Defect
Heavy corrosion to two wastewater storage tanks

Products Used


Sylmasta AB Original Epoxy Putty
Epoxy putty pushed into holes and cracks in tanks and pipes, where it will cure to a rock-hard material which permanently seals leaks

Liquid Metal Epoxy Coating
Brush applied coating which strengthens and protects metalwork by forming a new metallic, hard-wearing surface

Case Study PDF


Case Study Details


Luxury portable toilet trailers are mobile restroom facilities used for large outdoor occasions, such as music festivals and sporting events. They include flushing toilets, urinals, sinks with running water, mirrors and lighting, offering a much more comfortable experience than standard portable toilets.

Toilet trailers require no connection to permanent plumbing. Instead, the wastewater they produce is stored in holding tanks between the floor of the restroom and the undercarriage of the trailer. When the event has finished, the tanks are drained and the wastewater taken to a treatment site before the trailer is moved onto its next destination.

Constructing a portable toilet trailer is expensive, and so when one of the United Kingdom’s leading suppliers discovered holes starting to appear in the wastewater holding tanks of two of their units, they contacted Sylmasta for advice on whether a repair was feasible.

The plumbing, fixtures and fittings in each of the trailers were otherwise in perfect working order. The company therefore wanted to avoid decommissioning the two trailers if the holes in the wastewater tanks could be plugged and the weakened metalwork strengthened against future damage.

Sylmasta recommended a two-stage repair, starting with Sylmasta AB Original Epoxy Putty and finished with Liquid Metal Epoxy Coating. The first trailer was jacked up, enabling access underneath the wastewater holding tank. The metalwork was then ground down to remove rust, dirt and grime.

AB Original Black was supplied in stick format for the plugging of the holes. An AB Original Stick combines the resin and hardener pre-measured rather than in a tub of Part A and a tub of Part B, eliminating the need for weighing out and mixing separate components. This makes a repair quicker and easier.

The required amount of putty to fill a hole was cut from the stick and kneaded by hand. Once the putty had turned a uniform black colour but was still soft, it was pushed into the hole. After two hours, AB Original cured to form a rock-hard sealing material. Every hole in the tank was permanently filled in this way.

Once all the holes had been attended to, the entire bottom of the trailer – an area 1.3 metres by 2.5 metres – was painted with Liquid Metal Epoxy Coating. Also painted were the metallic box and pipe fitted to the bottom of the holding tank, through which wastewater was removed. Two coatings of Liquid Metal were brush applied, curing to form a smooth, metallic, hard-wearing surface.

This new surface repaired and strengthened the weakened metalwork to increase structural integrity. It acted as a protective shield against further external corrosion and encased the wastewater tank in a new outer shell, capable of containing the wastewater if the original metalwork became fully breached in future.

After the repair of the first toilet trailer was completed, the second was jacked up and fixed by following the exact same process. Each trailer could go back into service 24 hours after the second coating of Liquid Metal had been applied.

In total, 10kg of AB Original and 10kg of Liquid Metal were used to repair the two portable toilet trailers at a cost of under £800, representing a huge saving on replacing the units. The company are now planning to use the repair method on other units when they become weakened by corrosion, potentially extending the lifespan of their entire fleet by up to 10 years.

If you have an application you would like to enquire about, then please get in touch

Call: +44 (0)1444 831 459
Email: sales@sylmasta.com


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